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Posted: Sat May 06, 2006 10:14 pm
by T3Bunny
Well we have tried two differant coils.

At this point I am suspecting either the mods we used are wrong, or there is a defect on the board itself. I am finishing up a small jumper harness now, so I can test out a V3.0 on my own car. I should be further along with a real answer by the end of the weekend.

Posted: Mon May 08, 2006 5:08 am
by Paul_VR6
Double check those hardware mods again. No trouble here with the older V2.2 boards running a variety of 7pin and 3pin VW ignition amplfiers. If you suspect the VB you can always wire either of those in, dwell 75% fixed for the 7pin and dwell on for the 3 pin.

Posted: Mon May 08, 2006 9:17 am
by T3Bunny
I am no longer sure it IS an igniion issue. I had him setup everything with a 7pin module and still having the same exact issue. The datalogs are not as much help as I would have liked, due to only a NB fitted at the moment... But we are definatly seeing the motor go lean when it misfires.

And his boost gauge disagrees with the readings in his datalogs. I am suspecting the misfire is actualy a lean misfire as opposed to too much dwell.

As for the ECU mods, I used CdnDub's directions off the Tex. I am going to go back over them though. I am currently hacking into my own harness to go ahead and test everything out on a running car. Currently my car runs a V2.2 with a 7-pin IM. And I didn't make this first harness plug and play for either ECU like I have done since then... I think my car is going to get a new harness this week!