Odd reading from LM-1

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Minami Kotaro
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Posts: 42
Joined: Sun Sep 12, 2004 3:41 pm
Location: Somewhere in TN

Odd reading from LM-1

Post by Minami Kotaro »

I took the new engine for its first drive today, using the tune for my old engine. According to the LM-1, I was running at about 15:1 AFR. Good, good. But the engine starting bucking like it was way too rich and fouling the plugs. I datalogged, ran it through MegaTweak, and modified my VE map, which made it much leaner. The engine now ran great but ... the LM-1 now says 18:1 AFR during cruise. That can't be right, can it? The engine wouldn't run very well, it at all, if it were that lean, would it?

I think it must read leaner than it actually is. The sensor is reading the end of my 3" turbine exhaust (nowhere else to put it).

The LM-1 was calibrated correctly.
1967 VW Beetle
1915cc turbo ... only 3lbs so far
Controlled by MegaSquirt and EDIS
v2.2 board, MSNS-e 024s11
Check out my ongoing success story.
BottleFed70
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Joined: Fri Jun 24, 2005 2:22 pm

Post by BottleFed70 »

This is very common..

If there is a miss, the raw air and fuel gets dumped into the exhaust. The wideband O2 sensor reads this as being very lean as there is alot of unburnt oxygen.
1970 Ford Mustang
MSII, v3.0 PCB, v2.36 firmware, Megatune 2.25
Minami Kotaro
Helpful Squirter
Posts: 42
Joined: Sun Sep 12, 2004 3:41 pm
Location: Somewhere in TN

Post by Minami Kotaro »

This is very common..

If there is a miss, the raw air and fuel gets dumped into the exhaust. The wideband O2 sensor reads this as being very lean as there is alot of unburnt oxygen.

That's what I'm thinking.

Drove it around some today and it was saying around 15:1, then it started running choppy and saying 18:1, so I richened the map. It didn't help so we brought it home and pulled two plugs. One of them was wet and fouled and the other was pure white.

Got some investigating to do ...
Last edited by Minami Kotaro on Thu Sep 14, 2006 4:06 pm, edited 1 time in total.
1967 VW Beetle
1915cc turbo ... only 3lbs so far
Controlled by MegaSquirt and EDIS
v2.2 board, MSNS-e 024s11
Check out my ongoing success story.
Minami Kotaro
Helpful Squirter
Posts: 42
Joined: Sun Sep 12, 2004 3:41 pm
Location: Somewhere in TN

Post by Minami Kotaro »

Aha! One of the injector wires was pulled out of the relay board and continuously grounding against the case. Screwed it back down and it all works now. :D
1967 VW Beetle
1915cc turbo ... only 3lbs so far
Controlled by MegaSquirt and EDIS
v2.2 board, MSNS-e 024s11
Check out my ongoing success story.
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